Energy Saving Renovation Project of Circulating Water System of Shanghai Meishan Iron and Steel Co., Ltd.

This project involves ironmaking plant, steel plant and hot rolling plant, a total of 87 water pumps, the scope of the transformation includes improving the hydraulic performance of the pump, optimize the resistance characteristics of the pipe network. After the transformation, the key indicators such as flow and pressure fully meet the production requirements, and the average power saving rate reaches 16%, which has been highly recognized by Meishan Iron and Steel Co., Ltd. and gradually promoted in the whole plant of Meishan Iron and Steel Co., Ltd.

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Jiangsu Shagang Group Huaigang Special Steel Co., Ltd. Supply, Circulating Water System Energy Saving Reconstruction Project

This project involves the sintering plant, ironmaking plant, steelmaking plant, steel rolling plant, coking plant, power plant supply, circulating water system, more than 100 pumps. Among them, 74 pumps were retrofitted in EPC mode, replacing the original 78 pumps.

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Energy Saving Renovation Project of Circulating Water System of Hunan Valin Lianyuan Iron and Steel Group Co., Ltd.

The project involves the circulating water system of Lianyuan Iron and Steel Energy Plant, steel plant and steel rolling plant, with a total of 100 high-efficiency water pumps. After the transformation, the water pump runs well, the power saving effect is obvious, and the transformation results have been highly recognized by customers.

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Energy Saving Renovation Project of Water Supply and Circulating System of Lingyuan Iron and Steel Group Co., Ltd.

The first phase of the project involves 102 power plants, 9 coking plants and 15 ironmaking plants, totaling 126 water pumps. The key parameters such as flow and pressure remain unchanged before and after the technical reform, fully meeting the production needs of Lingyuan Steel. The average power saving rate of technological transformation reached 26.18 per cent, which was highly recognized by Lingyuan Iron and Steel.

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Anyang Iron and Steel Co., Ltd. Rolling Circulating Water System Energy Saving Project

This technical transformation involves the steel-making and steel-rolling workshop of Anyang Iron and Steel II, with a total of 27 circulating water pumps in 12 systems. After the transformation, the main flow rate, pressure and other key indicators of all systems are not lower than before the technological transformation. The average operating efficiency of the pump reaches 83-84%, and the average power saving rate exceeds 31%. The transformation effect has been highly recognized by Anyang Iron and Steel leaders and users.

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Energy Saving Renovation Project of Circulating Water System of Bayer Material Technology (China) Co., Ltd.

Bayer technical transformation project involves A547 system, the original system used in the pump for the German imported KSB water pump. This project has 10 technical renovation pumps, with an operating efficiency of 80%-82% before technical renovation and 88%-90% after technical renovation. According to the energy consumption per ton of water, the power saving rate is 15.2, the flow pressure and other indicators fully meet the production requirements, and the effect of technical transformation has been highly recognized by Bayer.

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Hubei Yihua Group Co., Ltd. Circulating Water System Energy Saving Reconstruction Project

Shanghai Rychen signed a strategic cooperation agreement with Hubei Yihua Group, responsible for the investigation of the energy consumption of the water system of Yihua Group's chemical plants, formulating energy-saving transformation plans, and implementing energy-saving technological transformation. After nearly three years of efforts, has completed a number of branches of the water system of energy-saving technology transformation, to meet the production needs of the premise, have achieved excellent energy-saving effect.

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Yang Coal Group Qilu First Chemical Fertilizer Co., Ltd. Circulating Water System Energy Saving Project

This project involves 18 water pumps, and the scope of transformation includes improving the hydraulic performance of water pumps and optimizing the resistance characteristics of the pipe network. After the transformation, the key indicators such as flow and pressure fully meet the production requirements, with an average power saving rate of 24%, which is highly recognized by customers.

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Energy Saving Renovation Project of Circulating Water System of Tangshan Ganglu Iron and Steel Co., Ltd.

In July 2016, Shanghai Rychen and Ganglu Iron and Steel signed an EPC contract on the energy-saving technical renovation of the circulating water system of the power plant. The construction was completed on January 18, 2017. The renovation pump operated stably and had significant energy-saving benefits.

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Masteel Group (Nanshan Mining, Gushan Mining) Circulating Water System Energy Saving Reconstruction Project

This project involves 3 circulating water systems of Nanshan Mining Company and Gushan Mining Company under the mining company, with a total of 9 pumps. In June 2013, Shanghai Rychen Environmental Protection Technology Co., Ltd. carried out energy-saving technical renovation on 4 pumps in 3# water supply pump room of Nanshan Mining Company's selection section, with an average power saving rate of 28%. Due to the obvious energy-saving effect, it was popularized in mining companies the following year. In August, 3 circulating pumps in 4# circulating water pump room of Nanshan mining company's mineral processing workshop and 2 circulating water pumps in 1# overflow pump room of Gushan mining company's mineral processing workshop were completed, the power saving rates were 19% and 26%, respectively.

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Hubei Xinye Steel Co., Ltd. Circulating Water System Energy Saving Project

This project involves several branch plants of Xinye Steel Co., Ltd., including steelmaking, power and oxygen production, 14 cooling systems and 22 high-efficiency water pumps. After the transformation, the water pump is running in good condition and the power saving effect is remarkable, which has been highly recognized by customers.

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No. 1 Furnace Air Preheater Renovation Project of Meigang 1422 Line

Shanghai Meishan Iron and Steel Co., Ltd. Hot Rolling Plant 1422mm Hot Rolling Furnace No.1 was put into operation in November 1993, and completed the technical transformation of combustion and cooling system in 2009. The fuel of the furnace is high-coke mixed gas, and regular burners are used for heating and continuous combustion control. The heating furnace is a walking beam heating furnace, and the furnace type is a three-stage heating side-to-side walking beam heating furnace. The heating furnace is divided into preheating section, heating section, heating section and soaking section along the furnace length from the charging end to the discharging end. In order to fully and effectively recover the waste heat of flue gas, a tubular air preheater is set in the flue.

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Meigang Hot Rolling Furnace "Reduce Oxidation Burning Loss Software Package" Project

Meishan Iron and Steel Co., Ltd. and Professor Xing Yuming of Beijing University of Aeronautics and Astronautics jointly cooperated in the technical transformation project of "Reducing Oxidation Burning Loss Software Package". The project was established in March 2017 and officially entered the project commissioning period in July, which lasted 9 months. In the course of the project, it has gone through several stages, such as manual debugging, installation of testing equipment, establishment of software package architecture, debugging and improvement of software package, and project evaluation. The results of the project are as follows:

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